EP 1130-2-510
13 Dec 96
APPENDIX E
EQUIPMENT FAILURE AND SYSTEM DISTURBANCE TELEPHONE REPORT
1. REPORTED BY DISTRICT: Tulsa District
TIME: 1300 DATE: 7 Jun95
2. PROJECT: Eufaula
EQUIP.FAIL.TIME: 0844 DATE: 7 Jun95
RETURNED TO SERVICE: 1500 DATE: 14 Jun95
4. DESCRIPTION OF FAILURE: Phase B of regulator power transformer failed blowing the
high voltage fuse on that phase. Protective relays for regulator tripped auxiliary relay 5c shutting
down the generator.
5. LOAD INTERRUPTED MW: 34 FROM: 0844 7 Jun95
TO: 1500 14 Jun95
6. CAPACITY OUTAGE MW: 30 FROM: 0844 7 Jun95
TO: 1500 14 Jun95
7. EFFECT ON CONNECTED SYSTEM: Loss of 30 MW of reserve capacity.
8. PROBABLE CAUSE: Defective transformer insulation.
9. CORRECTIVE ACTION: Transformer removed and taken to local repair shop by plant
personnel. Phase B was rewound and transformer reinstalled.
10. DEFICIENCIES: No known deficiencies.
11. REMARKS: 10 minutes before regulator transformer failure transmission line #2 (PSO line
to Stigler OK) tripped after a cross arm broke. The line relays operated properly (carrier ground
tripped line) leaving all three generators on line feeding lines 1 and 3. When the line tripped
generator voltage peaked at 14.2kv. I estimate unit will return to service the middle of next
week.
12. PARTIAL REPORT:
FINAL REPORT:
XXXX
NA = Not applicable
CALL TAKEN BY: Westmeyer
NK = Not known
E = Estimated
A = Actual
* = Mfg & Type
E-1